After BlueSpark treatment, the injection rate had increased by 1,260%. Follow-up acid treatment resulted in a combined 2,800% increase.

After BlueSpark treatment, the injection rate had increased by 1,260%. Follow-up acid treatment resulted in a combined 2,800% increase.
The disposal well of an E&P company was experiencing a continuous decrease in the injection rate, thought to be from fines in the produced water being injected that was plugging the screens. The well was designed for up to 10,000 bwpd and had reached 7,600 bwpd during its history.
In 2014, the rate dropped to 5,800 bwpd at 1,800 psi, prompting a screen wash and acid job to be done. The rate improved to 10,800 bwpd at 1,100 psi, but within two months the rate declined rapidly to 587 bwpd at 1,500 psi. The well was shut-in in February 2016.

Improve connectivity to the reservoir by clearing out blockages using electro-hydraulic pulsing technology.