CS 158
SCALE REMOVAL
PRODUCING WELL
OFFSHORE PLATFORM
NORTH SEA
SSSV

SSSV functionality restored

11 hours of treatment reactivated SSSV that failed inflow test twice in 12 months.

11 hours of treatment reactivated SSSV that failed inflow test twice in 12 months.

Challenge

The SSSV of the well of a major operator in the Danish North Sea had previously failed an inflow test and was reactivated by BLUESPARK® at that time. The SSSV was failing the inflow test again a year later and was believed to be in a stuck open position. It was decided to use BLUESPARK® again to clean scale from the SSSV to reactivate it.

  • Offshore conventional oil field
  • CaCO3 scale
  • Depth: 1900 ft (580 m)
  • Temperature: 62 °C (144 °F)

Solution

Remove scale from SSSV to restore functionality using electro-hydraulic pulsing technology.

  • The BLUESPARK® 275 tool with Fluid Hold-Up Tool (FHUT) was run on third-party E-Line to the treatment interval
  • Two complete passes, a pass over the flow-tube, and a station at the flapper of the SSSV were completed in a treatment time of 11 hours
  • Camera images were obtained to compare to images made before the BLUESPARK® treatment

Outcome

  • The SSSV was cleaned of CaCO3 scale and now passed the inflow test
  • Camera images confirmed that scale had been removed from the SSSV

Before BLUESPARK® Treatment

After BLUESPARK® Treatment

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