NSEA-SR-151 (Danish North Sea)
CHALLENGE
The customers’ SCSSSV had failed numerous times in recent years due to scale build-up. The SCSSSV had failed again, and camera images showed scale buildup and a possible damaged flow tube. The customer wished to clean the SCSSSV to be able to place an insert valve. Due to numerous successes with BLUESPARK® on past wells, the customer rush mobilized Blue Spark Energy to treat the SCSSSV.
SOLUTION
Remove scale from the SCSSSV using electro-hydraulic pulsing technology
•The BLUESPARK® 275 tool with a Fluid Hold-Up Tool was run on third-party E-Line to the treatment interval of the well
•Two pulsing passes were made over a 13 ft (4.0 m) interval in a treatment time of 6 hours
•An inflow test of the SCSSSV was performed, which passed
•The flow tube appeared to be functional, resulting in no requirement to set an insert valve
CONDITIONS
Depth: 1,800 ft (550 m)
Temperature: 35 °C (95 °F)
Treatment in 23° deviation section
OUTCOME
The SCSSSV scale was removed by BLUESPARK®, resulting in a successful inflow test and no need for an insert valve
Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.