NSEA-SR-151 (Danish North Sea)

CHALLENGE

The customers’ SCSSSV had failed numerous times in recent years due to scale build-up.  The SCSSSV had failed again, and camera images showed scale buildup and a possible damaged flow tube.  The customer wished to clean the SCSSSV to be able to place an insert valve.  Due to numerous successes with BLUESPARK® on past wells, the customer rush mobilized Blue Spark Energy to treat the SCSSSV.

SOLUTION

Remove scale from the SCSSSV using electro-hydraulic pulsing technology

•The BLUESPARK® 275 tool with a Fluid Hold-Up Tool was run on third-party E-Line to the treatment interval of the well

•Two pulsing passes were made over a  13 ft (4.0 m) interval in a treatment time of 6 hours

•An inflow test of the SCSSSV was performed, which passed

•The flow tube appeared to be functional, resulting in no requirement to set an insert valve

CONDITIONS

  • Depth: 1,800 ft (550 m)

  • Temperature: 35 °C (95 °F)

  • Treatment in 23° deviation section

OUTCOME

  • The SCSSSV scale was removed by BLUESPARK®, resulting in a successful inflow test and no need for an insert valve


Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.

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NSEA-PW-152 (Norweigan North Sea)

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APAC-IW-149 (Japan)