APAC-IW-149 (Japan)
CHALLENGE
A GeoThermal company in Japan was experiencing reduced rates in their injection wells due to silicon dioxide scale. They were looking for an alternative to the traditional treatment of rig operated mechanical dredging, hoping for better results with a lower cost and better efficiency.
SOLUTION
Improve connectivity to the reservoir by clearing out blockages using electro-hydraulic pulsing technology
A crane was used instead of the usual oilfield rig, reducing the carbon footprint
The BLUESPARK® 275 tool was run on third-party E-Line to the treatment interval
40 m (131 ft) of interval was treated in an operating time of 13 hours
The well was put back on injection and monitored
CONDITIONS
Depth: 800 m (2,600 ft)
Temperature: 120 °C (248 °F)
OUTCOME
The well was completed with zero safety incidents, zero non-conformances, and 100% operational efficiency
The operation was completed with a much-reduced carbon footprint as only a crane was required instead of a rig when compared to the traditional treatment method of mechanical dredging
The operation was also much faster than dredging, taking 1.5 days instead of 7 days (on the average)
The injection rate increased to as much as 12x the rate before treatment
The final stable rate was only slightly less that the original rate after completion 6 years earlier
Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.