CHALLENGE

The client had converted this well from a producer to an injector after 1 year of production. The well initially injected at over 300 b/d. The injection rate had fallen to below 100 b/d within 2 years.

After falling to 20 b/d a year later, an acid job returned the injection rate to 100 b/d, but that lasted only 3 months. The client was looking for a cost effective solution that would last longer.

SOLUTION

Improve connectivity to the reservoir by removing CaSO4 scale and clearing out blockages using electro-hydraulic stimulation technology.

  • The BLUESPARK® tool was run on tractor to the bottom of the lateral and then was pulsed at each frac port while moving uphole.

  • The well was treated in 13 hours of total operating time.

  • “Green” acid was bull-headed down the wellbore to the interval that had just been treated.

  • The well was put back on production and monitored.

Blue Spark Energy - case study MULTI-STAGE HORIZONTAL INJECTOR WESTERN CANADA

CONDITIONS

  • Measured Depth: 3,000 m (10,000 ft)

  • TVD: 1,500 m (5,000 ft)

  • Bakken shale

OUTCOME

  • The well saw an immediate increase in injectivity.

  • The average 3-month injection rate went from 2.2 b/d to 73.9 b/d (3200% increase).

  • The average injection rate for the 12-months post-BLUESPARK® was 148.3 b/d (6600% increase).


Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.

Previous
Previous

NSEA-SR-131 (North Sea)

Next
Next

NSEA-SR-129 (North Sea)