NAM-SR-121 (USA Permian)
CHALLENGE
The client’s well fluids had dropped by 50% during the past 2 years. Scale deposition was suspected to be in and near the perforations. No remediation had been done in 10 years. The client was planning a workover and required a remediation method that would improve lost fluid flow.
Based on adjacent wells’ production, the client was expecting increases of approx. 5 BOPD and 5 mcf/d gas. Payout was required to be less than 9 months.
SOLUTION
Improve connectivity to the reservoir using electro-hydraulic stimulation technology.
The reservoir was treated with BLUESPARK® to re-initiate production losses.
Approximately 40 ft (12 m) of perforated interval was treated with our wireline conveyed tool during a single day.
The client ran both the pump assembly and production tubing into the wellbore and began monitoring production rates. An immediate increase in production was observed.
CONDITIONS
Depth: 9,700 ft (2950 m)
Temperature: 145 °F (63 °C)
1st Bone Spring formation
OUTCOME
Data from the BLUESPARK® treated well showed a 3-month oil production increase from 6.2to 22.8 b/d (268% increase).
Gas production increased from 9.8 to 79.8 mcf/d in the same 3 months (714% increase).
The 12-month average rates correspond to a 250% increase for oil and a 510% increase for gas compared to the pre-stim rates.
Based on the results, the client is looking for other candidates in the field to remediate.
Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.