CHALLENGE

The client’s well fluids had dropped by 50% during the past 2 years. Scale deposition was suspected to be in and near the perforations. No remediation had been done in 10 years. The client was planning a workover and required a remediation method that would improve lost fluid flow.

Based on adjacent wells’ production, the client was expecting increases of approx. 5 BOPD and 5 mcf/d gas. Payout was required to be less than 9 months.

SOLUTION

Improve connectivity to the reservoir using electro-hydraulic stimulation technology.

  • The reservoir was treated with BLUESPARK® to re-initiate production losses.

  • Approximately 40 ft (12 m) of perforated interval was treated with our wireline conveyed tool during a single day.

  • The client ran both the pump assembly and production tubing into the wellbore and began monitoring production rates. An immediate increase in production was observed.

Blue Spark Energy - case study BONE SPRING FORMATION NEW  MEXICO, USA

CONDITIONS

  • Depth: 9,700 ft (2950 m)

  • Temperature: 145 °F (63 °C)

  • 1st Bone Spring formation

OUTCOME

  • Data from the BLUESPARK® treated well showed a 3-month oil production increase from 6.2to 22.8 b/d (268% increase).

  • Gas production increased from 9.8 to 79.8 mcf/d in the same 3 months (714% increase).

  • The 12-month average rates correspond to a 250% increase for oil and a 510% increase for gas compared to the pre-stim rates.

  • Based on the results, the client is looking for other candidates in the field to remediate.


Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.

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NAM-IW-122 (Canada West)

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NSEA-SR-120 (North Sea)