CHALLENGE

Client had a well with blocked perforation tunnels from fines circulated into the perforations during a workover. Oil production was down significantly, and all other attempts to clean out the perforations had been ineffective.

The client was willing to try a new technology to clear the perforations to help improve fluid flow into the borehole.

SOLUTION

Unblock the perforations and improve connectivity to the reservoir by using electro-hydraulic stimulation technology.

  • Unconsolidated sandstone reservoir was treated with BLUESPARK® to improve production.

  • No special tools or equipment were required on location to complete the remediation operation, other than third party E-Line.

  • There were 14 individual perforation clusters treated with BLUESPARK® in 8 hours of stimulation time.

  • Production rates and fluid levels were both monitored for comparison to pre-treatment values.

Blue Spark Energy - case study SAN JOAQUIN  BASIN CALIFORNIA, USA

CONDITIONS

  • Depth: 1,200-2,300 ft (360-700 m)

  • Rock type: diatomite

OUTCOME

  • Perforations were cleared, allowing for increased fluid flow into the wellbore.

  • Public data from the BLUESPARK® treated well showed an average production increase from 0.8 b/d to 7.6 b/d (comparing 3 months pre-stimulation to 3 months post-stimulation), an 850% increase.

  • The average rate for the first 6 months post-stimulation was 5.5 b/d, an increase of almost 600% versus the pre-stimulation rate.


Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.

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NAM-IW-111 (Canada West)

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NAM-SR-109 (Canada West)