NAM-PW-116 (USA California)
CHALLENGE
The client operates a small field under steam flood with declining oil production. Conventional stimulation techniques such as acid had yielded mixed and/or short term results. The client was interested in trying a cost effective technology that would potentially provide better and/or longer lasting results.
SOLUTION
Improve connectivity to the reservoir through a slotted liner using electro-hydraulic stimulation technology.
The client chose 5 wells to treat with BLUESPARK® to improve production.
The client selected the treatment zones from open hole logs, such that the total interval stimulated could be maximized in a single day of operation for each well.
Tubing was pulled and a bit-and-scraper run was done on each well.
The BLUESPARK® stimulation was completed on all 5 wells in 5 working days.
CONDITIONS
Depth: 650 ft (200 m)
Etchegoin Sandstone
Porosity 35%; Perm 5 D
OUTCOME
The wells were immediately put back on production and rates, pressures and fluid levels were monitored.
The total production for the 5 wells increased by 65% based on a 3-month comparison, while the water cut decreased by 5%.
Three of the wells saw increases of over 100%.
The total production for the 5 wells maintained a 62% increase for the 12-months following the stimulation.
Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.