CHALLENGE

The client operates a small field under steam flood with declining oil production. Conventional stimulation techniques such as acid had yielded mixed and/or short term results. The client was interested in trying a cost effective technology that would potentially provide better and/or longer lasting results.

SOLUTION

Improve connectivity to the reservoir through a slotted liner using electro-hydraulic stimulation technology.

  • The client chose 5 wells to treat with BLUESPARK® to improve production.

  • The client selected the treatment zones from open hole logs, such that the total interval stimulated could be maximized in a single day of operation for each well.

  • Tubing was pulled and a bit-and-scraper run was done on each well.

  • The BLUESPARK® stimulation was completed on all 5 wells in 5 working days.

Blue Spark Energy - case study STEAM FLOOD CALIFORNIA, USA

CONDITIONS

  • Depth: 650 ft (200 m)

  • Etchegoin Sandstone

  • Porosity 35%; Perm 5 D

OUTCOME

  • The wells were immediately put back on production and rates, pressures and fluid levels were monitored.

  • The total production for the 5 wells increased by 65% based on a 3-month comparison, while the water cut decreased by 5%.

  • Three of the wells saw increases of over 100%.

  • The total production for the 5 wells maintained a 62% increase for the 12-months following the stimulation.


Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.

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NAM-SR-117 (Canada West)

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NAM-SR-115 (USA Permian)