CHALLENGE

Client well continually developed calcium carbonate scale (CaCO3) in the perforations, reducing production. Client was interested in using the BLUESPARK® tool to remove the scale from the perforations and to test scale removal from inside the casing. Determine the optimal pulsing rate for removing scale in casing, to maximize efficiency.

SOLUTION

Remove scale and improve connectivity to the reservoir using electro-hydraulic stimulation technology.

  • A pre-BLUESPARK® multi-finger caliper log was run to identify the thickness of scale in casing.

  • The perforated interval of the well was stimulated with BLUESPARK®.

  • A post-BLUESPARK® multi-finger caliper log was run.

Blue Spark Energy - case study CALCIUM CARBONATE SCALE TEXAS, USA

CONDITIONS

  • Depth: 1,800 ft (550 m)

  • Sandstone formation

OUTCOME

  • The post-BLUESPARK® multi-finger caliper confirmed that 100% of scale was removed at a pulsing rate of 60 pulses/ft.

  • Oil production increased from 4.8 b/d to 8.5 b/d when comparing the 3-month pre-BLUESPARK® to 3-month post-BLUESPARK® rates.


Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.

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NAM-PW-116 (USA California)

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